“Getting 5029 and 4953 back to Base”. 5Z27
19th/20th October 2009.
One of the enjoyable trips that can be
encountered when participating in heritage railway galas can be the movements
to get mainline registered locos on and off the railway concerned.
This creates a lot of interest and publicity for the steam movement usually
on a weekday, witnessed by the unsuspecting public waiting on station platforms
and vantage points, plus the enthusiasts who get to hear through the grapevine.
Such an event was the Monday 19th and Tuesday 20th October 2009 when 5 of
our support crew alongside Nigel a representative for 4953 “Pitchford
Hall” prepared both locos on the Monday for the Tuesday return working
to Tyseley from Minehead after the West Somerset Railway gala.
Monday morning started with me being up at 04.00 to be picked up by our Responsible
Officer for the trip Ian. We departed Shrewsbury by train at 05.21 for Taunton
via a change at Birmingham New Street. With an uneventful trip we arrived
at Taunton Station at 08.42 and after a short while we were picked up by Richard
and Ben, another two of our crew and were driven onto Minehead. We arrived
in Minehead shed yard by 09.30 and were greeted by Andy Forster the West Somerset
Railway’s Chief Engineer.
We unloaded our bags into our support coach, whilst one of the WSR staff had
been clearing the ash from the smokebox and grates on both locos. In steam
alongside us was 6024 “King Edward V1” about to head onto the
mainline to go to Kidderminster (SVR). After a quick cuppa, Ian and I went
off into the High Street to Somerfields to stock up on food provisions for
the next two days.
On our return 6024 had gone with its Support Coach. I changed into my overalls
before setting about topping up the lubricator and then oiling up all around
the outside oil points and axleboxes under Ians guidance. Minehead’s
Class 03 Drewry diesel shunter propelled us down onto the pit so that hopper
ashpans could be emptied and a fire was put in both locos.
Churchward 2-8-0 3850 was running up and down the platform with the WSR Driver
Experience turns bedding the novice crews in prior to running down the line
that afternoon.
Both fires were brought round to ensure we had enough steam for Richard to
carry out the Fitness to Run Exams later in the afternoon on both locos and
our POB (Private Owners Brake), this test basically ensuring everything is
safe to go out onto Network Rail. Ben and I continued the oiling up process,
then with some time spare after a break for lunch and a cuppa we started cleaning
the wheels, frames and motion of our loco and tender.
With the Fitness to Run exams and paperwork completed Richard left us at teatime
to head off north. We went onto the pit to complete the task of oiling up
the inside motion, eccentrics, crosshead etc, places where there was not much
room despite being in a pit! The position of the motion up in the frames makes
some points difficult to access. Whilst all work on a static loco a “Not
to be Moved Board” must be displayed on the outside of a loco and the
handbrake on and wheels scotched to prevent any movement preventing any injuries.
A hose pipe had also been dropped in the tender to top up the water. Our other
crew member Peter arrived late afternoon via the local bus from Taunton.
After a shunt with both locos in steam, we had everything ready and in position
for the next day with 5029 piloting 4953 and support coach trailing. I had
a welcome shower in the WSR messroom. Once we were all cleaned up by 6.30pm
we were all strolling down the prom westbound to a local restaurant, where
we enjoyed various steak and fish dishes and were able to relax for the evening.
Once back at base we banked the fires up for the night and received our briefing
off Ian for the following day then settled into our sleeping bags on the cushions
for the night at a reasonable hour.
I managed a little sleep until we were roused at 06.00 with the lights going
on. After a quick cup of coffee Peter and I made some attempts to liven up
the fire as we were due to go off shed at 8.00 and both locos had to be coaled
by a JCB before we left. Ian then cooked us up a breakfast which we soon devoured,
then I made sure our tail lamp was on the rear of our coach and both headlamps,
one of which is the high powered electric one which had been on charge, were
on the brackets on the front running plate. Electric cables were disconnected
and put back into the coach workshop.
The tank in support coach had been topped up with water and the hosepipe was
now taken out. Ian made a quick check around, some oiling points were topped
up, all tools were ensured to be back into the coach.
The JCB filled up both loco tenders with coal, this took some time so we did
leave Minehead with WSR crews about 5 minutes late with Ian riding on Nunney
and our Ben joined Nigel Spur on 4953.
Peter and I tidied up in the coach, cleaned ourselves up then rested on the
cushions on the trip down to Bishops Lydeard.
When we arrived there, the weather was cloudy and drizzly. We ran through
the platform. Soon the West Coast crews had deposited there bags in the coach.
John Williams was to drive the “Hall” and Jim Clarke drive the
“Castle” with Ray Poole to firing. We reversed down onto the water
column to fill both tenders in the time we had, said goodbye to Andy Forster
and the WSR, who asked us to come back again.
We departed and after a few miles we were on the site of the new triangle
and new halt, all being constructed taking in part of the ex Barnstaple Branch
alignment. Receiving a yellow on the approach to the new connection at Norton
Fitzwarren, we ran onto the main line at 09.43, dead on time.
Past the site of Silk Mill Crossing, now an overbridge, and the large new
engineer’s sidings on the down side. We ran into Taunton’s platform
2 to let our WSR pilotman get off and the passage of a Cross Country Voyager
to go in front of us. After five minutes we were off on the up relief line
and had an uninterrupted trip to Bristol. We were restricted to 50mph. We
were held at Bristol West Junction as we were eight minutes early, then we
were allowed into Platform 4 of Temple Meads under the overall roof. We were
allowed 33 minutes to water both locos, so we soon had the hoses rolled out
and standpipe out to the hydrant just outside the metal gate and we became
a centre of attraction for dads and boys alike. The Hall took water first
via its tender top filler then we had a chance of a cup of tea, water pressure
was good, we had a slight problem turning the hydrant off before we could
transfer our hoses into the low level filler on the Castle.
With 5 minutes to go Ray Poole was happy we had sufficient water to carry
on, so water was turned off and hoses were quickly uncoupled, rolled away
and put back in the coach.
I requested a run on the ‘Hall’ from Bristol, once we were away
past Barton Hill Depot it was obvious the Castle was going to do most of the
work. We climbed the long pull up from Dr Days Junction, through Lawrence
Hill up to Filton Abbey Wood, then the right hand curve on through Bristol
Parkway. I stood behind driver John Williams with Nigel Spur on the firemans
side.
From here on we were frequently confronted by Double Yellows, so many trains
in front so at Hullavington we got the feather into the loop for ten minutes
where we were able to allow an HST and a Cross Country Voyager get by. Ray
Poole and our Ben Jervis on 5029’s tender in front brought coal forward.
Once away we soon had the call of ‘tunnel’, the firehole doors
closed, blower on as we approached Chipping Sodbury Tunnel, brick built in
1900, all 2 ½ miles (4kms) of it, running down at 1 in 300.
Going through a long tunnel with steam is an awesome feeling, the movement
and sense of power and speed with the incredible noise of the exhaust of both
engines echoing down a long tube you are in the middle of. I thought it was
never going to end and we were going down into “Andantes Inferno”
and the Devil himself. Then suddenly we broke out into the daylight and your
body could relax as we ran down to Wooton Bassett Junction, where the line
from Bristol via Bath came in.
Within ten minutes with both locos in their stride we were whistling for the
approach to Swindon, that great birthplace that went into the sky. Whistling
to make sure the Great Western’s legacy was not forgotten, we rattled
over the series of points and crossovers passing the remains of Swindon’s
once fine locomotive workshops and accelerated through the station. From here
on we were galloping away nicely as the sun broke through the drizzle for
a while until we were signalled into the loop at Challow, to let a Voyager
go by. Away again we were held for a short while on the east to west curve
off Foxhall Junction to Didcot North and the run up to Oxford.
We had to slow to 5 mph for the tight clearances at Culham and Radley platforms.
Just south of Oxford we had to wait a short while for the movement over the
up main line into the loop at Hinksey where we were booked to take water.
Once in the loop and the marker post reached we again soon had the hoses out
over the fence only to find a car parked over the hydrant. Fortunately the
car owner was close at hand and the car was promptly moved.
We were allowed an hour here to fill both locos, as a procession of Container
trains, Turbostars, Voyagers etc passed us by, it was a very busy time. I
rode the Castle from here on, Ray Poole had contacted control to say we were
ready to leave as we eased up to the red signal, only to be told there was
a points failure at Aynho Junction and we would be held a little longer, so
I had time to bring more coal forward.
A Ballast train eased past us and waited in Oxford’s down platform.
Once we had a yellow signal we eased through Oxford station in the middle
road where we were held again until we could proceed in front of this ballast
train. Again we had a succession of Turbos coming and going, and we had a
sudden downpour in which my back got soaked as we had no tender storm sheet
on.
We left Oxford about twenty down and still got a succession of double yellows
for some way.
Jim Walker was driving Nunney fully opening her up again, whilst Ray was frequently
keeping the back end of the firebox constantly filled up, at times firing
over the flap and at times having both injectors working, we were not short
of steam. Occasionally now we did hear the Hall open up and try to push us,
but not for long.
The rain had eased off as we approached Aynho and by Banbury we sailed through
our booked stop, also Leamington we kept going to cut our time back. We were
soon on Hatton Bank and made easy work up to the top. A fast run ensued through
Lapworth, once the site of water troughs and by Dorridge, Ray started to get
rid of some rubbish, dusty coal. Just past Acocks Green we were held at a
Red until we got the feather which allowed us to run down into the confines
of Tyseley Depot.
Ray also phoned ahead to ensure the road was set to get us back into Tyseley
Steam Trust HQ. We arrived back into the depot around 20 minutes late at 17.05.
Once we parked up, handbrakes were put on, fires were cleaned, injectors put
on to take the water well up the glass, lamps and tools were put away and
locked up.
We said goodbye and thanks to the West Coast crews, got ourselves cleaned
up and changed to set off home. Peter drove, Ian, Ben and I took the local
bus to New Street and our trains home.
All we have to do now is make a start on the list of jobs noted for the winter
maintenance period, any new keen willing volunteers to join us and help with
running and maintaining 5029?
David Giddins, 5029 Support Crew Member.
Nunney Castle participated over a four
day Gala with a GWR theme, Prelude to GW175 next year, sharing duties with
visiting locos 6024 “King Edward V1”, 4953 “Pitchford Hall”,
7802 “Bradley Manor”, 9466 and 5224 alongside resident locos 3850,4160,
5542, 5553 ,6695 and 9351.
I arrived at Minehead on the Saturday morning, with another fellow Dave in
our support crew.
The rest of the gang were already cleaning 5029, which was due to double head
with my other favourite loco 7802 “Bradley Manor” the 11.15 out
of Minehead.
I knew 7802’s support crew well, and we had a lot of banter about which
loco was going to push or pull the other. It was a wet drizzly morning but
we had a good trip to Bishops Lydeard and back, I requested if I could go
down as loco rep on this trip, the WSR crews handled both locos well.
Second trip of the day had problems with a clinkering fire on 5029, but so
did the “King”, so the planned last train of the day to be double
headed never materialised. 6024 was late with the last train so 5029 worked
back light engine very late.
Nunney had a quick disposal and a small fire remade. We had to get our late
meal walking through a MacDonalds drive in up the road as everywhere had stopped
serving food.
So we retired to bed around midnight and were up again at 06.00, oiling up
whilst the WSR crew actually put another new clean fire in our loco, when
pressure was up it was turned on the new turntable.
I rode on the cushions on the first train behind Nunney down to Bishops Lydeard
, our loco having a WSR Inspector on board, and beyond to the WSR current
extent at the new triangle under construction, before Norton Fitzwarren.
Here 6024 was on the rear of our train to haul us back non stop to Minehead,
now that the sun had come out. Nunney would return all the way non stop.
I again rode our engine on the afternoon trip with two different friendly
crews with no problems arriving back on the last train of the Gala at Minehead
at 19.00. The loco was uncoupled and parked alongside the shed, where we raked
through the fire, put the injectors on and filled her right up, put her to
bed, lamps and tools being put away and support coach locked up, we were on
our way home at 20.00 hrs.
We would like to thank everyone involved at the West Somerset Railway over
the 4 day Gala for there friendliness, help and cooperation.
Dave Giddins,
5029 Support Crew.
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October 3rd & 4th 2009.
Three of the support group seen
here relaxing during the preparing of 5029 for the days service on the Railway.
From left: Ben C, Steve T, and Dave
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